FedEx Express Flight 14
FedEx Express Flight 14 was a scheduled cargo flight from Singapore to Newark, New Jersey, via Malaysia, Taiwan, and Alaska. On July 31, 1997, the aircraft flying this route crashed during landing on its final segment at Newark International Airport, inverting and catching fire, injuring all five people on board.
Summary
Flight 14 crashed while landing on runway 22R at Newark Airport on July 31, 1997. The flight originated in Singapore with intermediate stops in Penang, Malaysia, followed by Taipei, Taiwan, and then Anchorage, Alaska. In addition to the Captain and First Officer there were three passengers on board, including one riding in the jump seat.During the flight, the pilots were concerned that they would have little stopping distance after landing, and the captain said that he wanted to put the aircraft down early on the runway. The aircraft had departed with one thrust reverser inoperative, and the pilots knew of incidents in the aircraft's maintenance log where the auto-brakes had failed to activate during landings. They had also misinterpreted the runway data, and so believed they had less stopping distance than was actually available.
The landing was normal until the beginning of the flare phase. The MD-11 touched down, bounced, and rolled to the right. On the second touchdown, about later, the right gear snapped and the No. 3 engine contacted the runway, with the right roll continuing until the right wing spars broke. The aircraft came to rest off the right side of the runway, inverted, and on fire. All five occupants escaped through a cockpit window. The airplane was destroyed by fire.
Aircraft and crew
The aircraft, named Joshua by FedEx, construction number 48603 and line number 553, was a McDonnell Douglas MD-11F freight model, powered by three General Electric CF6-80C2D1F engines. Registered in the United States as the aircraft was delivered new to FedEx in September 1993. Prior to the crash, the aircraft had a total of 13,034 flight hours and 2,950 flight cycles, and had been involved in two prior incidents. In January 1994, it sustained underbelly damage during a bounced landing at Memphis International Airport. Then in November 1994, the aircraft was involved in a tailstrike at Anchorage International Airport. Permanent repairs were made from the Anchorage incident within days of the tailstrike, and permanent repairs to the Memphis incident were made at the next C check in August 1995.The captain was 46-year-old Robert M. Freeman who joined FedEx in 1988 when it bought Flying Tiger Line, which he had previously worked for since 1978. Freeman had logged a total of 11,000 flight hours, including 1,253 hours on the MD-11. The first officer was 39-year-old Donald E. Goodin, who had been with FedEx since 1994, having served as a former U.S. Air Force pilot from 1977 to 1994 and had 3,703 flight hours, though only 592 of them were with FedEx. Goodin only had 95 hours on the MD-11.